Published: | 2010-02-23 |
Manufacturer: | Scratch |
Brief:
In checkin' me club's flight cards for t' last 2.5 years, me hearties, matey, ya bilge rat, I find that thar have been 8 MMX
launches. Begad! Ahoy! All o' them were done by me. Avast! Well, blow me down! I have tried t' see if thar be any interest in an informal MMX contest o' some
type on several occasions and thar be not. Begad! In delvin' a bit deeper, matey, I learned that MMX was nay disdained because of
its diminutive size, it was shunned because o' t' hassle, real and perceived, shiver me timbers, arrr, o' flyin' them. Aye aye! Avast, arrr, me proud beauty! That be an attitude I
shared myself. Ya scallywag! Well, me hearties, blow me down! Every time I thought about buildin' or flyin' one, arrr, I usually gave it up as too much hassle.
That is especially true o' t' ground support equipment. Avast! Blimey! T' silo launchers are problematic and I have had only one good launch off o' one. Ya scallywag! Blimey! T' rest o' t' time I have had t' kludge somethin' together, me hearties, ya bilge rat, cross me fingers and hope it works. Begad! Blimey! It sometimes even does.
This is nay t' say that thar are nay some great MMX GSE ideas out there. Well, blow me down! Begad! There are. Ahoy! Well, blow me down! They just don't strike me as worth t' effort. Aye aye! I finally decided t' see if I could design somethin' t' take some o' t' hassle out o' it and make it fun. Begad! Avast, me proud beauty! In effect, me hearties, with a minimum o' effort, I want t' be able t' treat an MMX rocket like any other. Avast, me proud beauty! Begad! Go out t' the assigned pad, me hearties, hook it up, walk away and have reasonable confidence that t' rocket would launch. Begad! I wanted t' be able to do this without lengthy preparation o' special consumables. Arrr! In order t' do it, I be willin' t' invest some time, effort and loot into makin' such a system.
T' basics that I wanted t' accomplish are these:
Construction:
T' first step in this grand project be t' get out an MMX igniter, measure it and make a drawin' o' it in Autocad. I measured t' 1/16" and estimated t' 1/32" I think it will be good enough for me purposes. Ya scallywag! Well, blow me down! I wanted t' DWG files o' t' various igniters I want t' plan for t' use as blocks in t' drawin' files help me draw up t' ignition system. Arrr! Ahoy! I also wanted t' have a half decent chance o' havin' t' thin' work when I got through. Avast! Arrr! I also cracked open t' plastic case and made a drawin' o' t' naked igniter. Blimey! Begad! With that done, I could start drawin' up the head.
I had liked what I had seen o' several ideas that used a slot t' support t' igniter and that was a part o' the idea as well. Aye aye! That bein' t' case, t' first thin' was t' come up with t' arm that provided t' support. Avast, me proud beauty! Ya scallywag! I decided on 1/4" plywood as t' basis for t' framework. Aye aye! I picked it for dimensional stability and because it is an insulator. Most important, though, ya bilge rat, it has laminations oriented at different angles so that shear should nay become an issue. Arrr! This was because I planned on a relatively skinny support, me bucko, me hearties, for reasons which will later become apparent.
I opened up Autocad and drew up a support arm that had a slot that be just a touch bigger than t' plastic encased igniter. Ya scallywag! At this point I did nay concern myself with length, only t' part that would support t' igniter. Avast! Blimey! I then printed out this simple drawing.
Although t' support beam would ultimately be o' plywood, shiver me timbers, I did nay use plywood at this stage. I chose instead a scrap o' 1/4" balsa since it would be easy t' whittle on and adjust and because it happened t' be handy. The template be trimmed a bit and then applied t' t' balsa with a glue stick. Avast! Ahoy! T' rough piece be then taken t' t' belt sander and t' profile was trimmed down t' t' outer edges o' t' template. Begad! Ahoy! With t' outer edges takin' place, me bucko, a razor knife was used t' carve out t' igniter slot.
Later that night, arrr, shiver me timbers, it was time t' examine t' first fruits o' t' project and I spread me stuff out on the kitchen table after t' Mrs. Blimey! had gone t' bed. Begad! Blimey! Blimey! I put in t' plastic igniter ans was glad t' see it fit; with me doing t' measurin' and cutting, such things cannot be assumed. Ya scallywag! I also test fitted t' stripped down, shiver me timbers, matey, paper clad igniter and it fit as well.
One o' t' problems I had experienced with other MMX systems was t' attachment o' t' microclips. Avast! My scheme was t' get rid o' t' "micro" altogether and replace it with "macro". Ya scallywag! I found a plastic clamp at Lowes that seemed t' fit t' ticket and tried it on t' support t' plastic igniter. Ahoy! Ahoy! At first blush it seemed t' work. Well, blow me down! Looking at it from t' top, me hearties, though, thar be a slight problem. T' grips on t' clamp were just a touch wider than t' slot. For t' ultimate plan, they needed t' fit flat within t' slot.
Before doin' any adjustment, though, arrr, ya bilge rat, I wanted t' try it with t' naked igniter. Avast, me proud beauty! Arrr! I slipped it into place, oriented 90 degrees from t' way t' plastic one had been, matey, and made sure t' leads extended on either side o' the support. T' clamp was then placed, shiver me timbers, much lower down this time, arrr, pinnin' t' leads t' either side o' t' support arm. Ahoy! I then spent some time fussin' with it. Key t' makin' me scheme work was t' degree o' stiffness o' t' igniter in this orientation. Ya scallywag! Ya scallywag! It seemed t' me that t' clamp was sufficiently tight t' hold it in place without any wiggling.
With t' information I had gotten thus far, I went back t' Autocad and widened t' slot by 1/32" on each side.
To provide electrical contact, I intended t' use a pair o' brass pieces, one on each side o' t' launch head. each would be primarily vertically oriented so that a naked or standard ingniter could be set in place with one lead clamped t' either side. Aye aye! Avast, me proud beauty! Blimey! I also intended t' fold a small piece o' brass over t' top t' catch t' leads on t' classic MMX igniter.
I went into Autocad and drew up a plan for t' brass pieces assumin' that I would be usin' 1/2" wide brass. T' lines for foldin' and cuttin' were marked interchangeably. Avast! A copy was then printed, me bucko, cut out and taped t' a piece of 1/2"x0.016"x12" piece o' brass. Begad! A cutoff disk on a Dremell tool was then used t' cut t' piece t' length and slice t' part that would be folded back. A pair o' pliers be then used t' make t' bends and folds. Ya scallywag! T' folds were nay completely bent into shape under t' theory that some finaglin' would be needed and I wanted t' fatigue the metal as little as possible. An identical piece be then cut and formed and t' pair was test fitted into t' head.
Solderin' is nay one o' me strong skills, and that's puttin' it kindly. Arrr! Even so, I felt obligated t' provide the electrons with a path t' get t' t' brass contacts. Begad! I took a length o' speaker wire, me bucko, stripped t' ends and then soldered a lead t' t' back o' each o' t' contact plates.
In order t' accommodate t' solder on t' backs o' t' contact plates and allow them t' lie flat, I had to excavate a cavity on either side o' t' head. Well, blow me down! Begad! It be done by trial and error with an ambiguous head on t' Dremmel. Avast! Ahoy!
Since this was merely a proof o' concept prototype, I did nay take t' trouble t' fasten t' plates t' t' head in a "good" manner. Arrr! Instead, me bucko, I just epoxied them into place and clamped them t' set. This proved t' be a mistake since some o' t' epoxy developed and unhealthy relationship with t' clamp and t' removal o' said clamp distorted things.
Several tests were made with t' prototype and I found that t' concept did work but that thar were some problems with execution. Ya scallywag! Aside from t' nay so durable balsa used as t' head, t' method o' attachin' t' wires t' the plates and t' plates t' t' head were also problematical. As I considered how t' deal with these issues, matey, I turned my attention t' t' "guts" o' t' project.
My intention all along be t' develop a series o' racks for various types o' rockets me club may fly. Avast! I wanted t' standardize as much o' t' design as possible. I had decided early on that each rack would be mounted on an identical steel sawhorse. Ya scallywag! Ahoy! T' that would be fastened a "box" that would contain whatever wirin' was needed and on t' "box" would be mounted t' individual launch heads. Well, blow me down! After lookin' at lots o' different options for the "box", I decided t' try usin' NEMA type 1 electrical troughs. For t' MMX rack, I ordered a 4"x4"x48" trough with a hinged cover and a pair o' endcaps t' go with it. Begad! I specified that I did not want knockouts.
I wanted t' go ahead and prime t' box and knew that me normal Kilz primer would nay be a good choice. Blimey! Ya scallywag! Based on some advice, ya bilge rat, me hearties, I purchased Dupli-Color automotive white primer and went t' work spraying. I smartly learned that while t' primer adhered well, a lot was needed for full coverage. I emptied a can and still plenty left t' go.
Rather than spend more in primer than t' box cost, I decided t' brush on some gray primer made for metal applications. Avast! Ya scallywag! I bought a gallon since I have several projects on which t' use it and because it was nay available in smaller sizes. Avast, me proud beauty! I brushed on t' first coat and let it dry overnight. T' end caps were painted as well.
T' first coat o' gray primer be rather streaky (but much better over t' surfaces that had received t' white spray primer first) and a second coat was applied t' all t' pieces. It came out much better.
A day after t' second coat o' primer was applied, I mounted t' end caps. Aye aye! Each one required 3 bolts I used 1/4x3/4 along with a lock washer. Blimey! Ya scallywag! When in place, t' caps greatly increased t' rigidity o' t' trough.
As mentioned before, t' base o' me system was t' be a commercially available steel sawhorse. Blimey! Blimey! I chose t' one made by Task Force because it seemed sturdy, already had some holes drilled about where I would want them, had adjustable length legs and because it happened t' be what was for sale at me local Lowes.
T' larger holes in t' sawhorse turned out t' be just right for 5/16" bolts. Begad! I assumed that each base would have a pair o' such bolts t' fasten t' box above. I saw a potential problem, though o' t' bolt slippin' out through t' hole while hands were occupied handlin' t' box. Blimey! Begad! I kept askin' about some sort o' "retainer" to keep them from slippin' out. Ya scallywag! I had just about decided t' try and fit a little rubber O rin' on t' shance t' keep it from slippin' through when somebody mentioned an "E clip". That turned out t' be just t' ticket. Arrr! T' bolt be slipped through t' hole and t' clip be popped into place at t' base. Begad! It did what I wanted and freed me hands from havin' t' keep t' bolt in place while fumblin' around with t' box.
To hold t' box onto t' sawhorse mounted bolts, me bucko, I wanted t' use wingnuts that could easily be removed. Begad! I also added a fender washer t' t' system t' spread t' load out a bit if t' assembly were t' be picked up by t' built in handle on t' sawhorse. Begad! Since I was nay yet ready t' mount t' box, I just stored t' washers and wingnuts in their eventual place o' residence.
T' bolts on t' base are spaced 30" apart so I drew a light line down t' centerline o' t' bottom o' the trough and made marks for t' bolt holes at that spacing, arrr, shiver me timbers, centered betwixt t' ends. Aye aye! T' holes were then drilled with a 5/16 bit.
T' system was now ready for me t' test fit t' box on top o' t' support. As such, I undid t' wingnuts and removed t' fender washers and was pleased t' see that t' bolts did nay then fall out. Begad! So far, so good. I set t' box on top and t' holes lined up t' t' bolts...mostly. Avast, me proud beauty! Ya scallywag! There was a bit o' tightness at one end and t' box was forcing t' bolt t' lean. Arrr! For grins, I put on t' washers and wingnuts and tightened it down part o' t' way. I then lifted the rack by t' carryin' handle and it seemed t' idea be sound so far but needed a little more work.
One o' t' things I noticed is that t' bolt stuck up farther than I liked on t' inside o' t' box. I decided t' use a 3/4" length instead o' t' full inch. Avast! Begad! Accordingly, I popped t' e-clip off and substituted a shorter bolt. Ya scallywag! I had also noticed that t' bolt tended t' turn as I tried t' tighten t' wingnut. T' remedy that I added a star lock washer under t' bolt head.
Another problem I noticed is that I must have gotten t' spacin' for t' holes in t' box just a wee bit off. Arrr! On bolt was tilted t' an angle when t' box was put one and t' nut could nay be completely tightened. Begad! I tried t' fit a nibbler into t' hole but t' head would nay quite fit so I took a round file and opened it up a bit. I was then able t' slip t' head o' t' nibbler in and took a single bite out o' t' hole t' let t' bolt sit more upright. Ya scallywag! T' box was then put back into place and this time it went down flush and t' wingnut took held it flat.
Another thin' I wanted t' change was t' screws that held t' hinged cover closed. Aye aye! These were simple screws that I KNEW would pop out and be lost in t' field since I wanted t' be able t' use t' box for storage. Ahoy! Arrr! As such, I ordered some knurled headed screws from Grainger t' replace them. I also ordered some split rings t' keep t' screws from pullin' all t' way out o' t' lid. Begad! When they came in, matey, shiver me timbers, all three screws on t' cover were replaced.
I had decided that t' rack would have 6 launch pads spaced 8" apart. This was tighter than I liked but I didn't want t' box t' be longer than 48" longs for transport. Avast, me proud beauty! I drew a line down t' center o' t' cover and marked 6 places evenly spaced betwixt t' 2 ends. I then drilled 5/16" holes at each station.
T' basic support o' each o' t' heads be t' consist o' a 2" long, arrr, 5/16" bolt. Blimey! Ya scallywag! Blimey! I added a washer to distribute t' force and a lock washer t' keep t' bolt from spinnin' as t' exposed side is manipulated. Begad! T' hold the bolt fast from t' top side, another washer and and nut were placed and t' assembly tightened down. Begad! Well, blow me down! Blimey! A pair o' nuts was then put onto t' upper side and turned down approximately halfway. Well, blow me down! T' purpose o' t' twin nuts is t' be able t' lock them against each other and set t' height. Begad! Blimey! Next came a pair o' SAE washers and a wingnut. T' washers are t' sandwich t' actual launch head. This process was repeated for all six stations.
As t' actual base and box were bein' built, me bucko, I kept workin' on t' design o' t' launch head, shiver me timbers, makin' some changes based upon t' original prototype. Ahoy! Aye aye! Blimey! On t' next set o' prototypes, I used plywood, a much more durable product than balsa but t' trade off is that it does nay whittle as easily t' make adjustments. I printed up new templates for 10 heads rough cut them with a jigsaw, shiver me timbers, sandin' them down t' t' outer profile. Ya scallywag! T' notch for t' igniters be rough cut with t' same jigsaw; thar was little uniformity except that I (mostly) stayed within t' lines. Finishin' down t' the lines be done with a combination o' X-acto, file and sandin' stick and eventually, they were all pretty standard.
An issue that had nay been addressed in t' previous prototype was t' securin' o' t' MMX launch rod. Ahoy! Blimey! I wanted somethin' more secure than just a hole drilled into t' plywood. Blimey! I wanted t' head t' retain t' rod. Avast! Blimey! I came up with an idea and ran it past several people with much more mechanical experience than me. Begad! T' answer I kept gettin' was that "it might work; try it and see." That turned out t' be some work and an excuse t' acquire some new tools.
I bought a 3 foot length o' 1/8" brass tubin' t' receive t' rods. Ahoy! A cut off wheel on a Dremmel tool was used t' cut 10 pieces, arrr, each an inch and a quarter long. Avast! Begad! There was some sloppiness here and some turned out longer and some shorter but, shiver me timbers, in general, ya bilge rat, their length was t' same as t' depth o' t' launch head.
A guy at Quality Fasteners, arrr, ya bilge rat, a local screw and bolt place, ya bilge rat, gave me t' idea for securin' t' brass tube in place. Up until now, arrr, me mind had gone off in a completely different and much more complex direction. Well, blow me down! For each piece o' brass, I obtained 2 nylon harnesses that seem t' be designed t' retain wire. Each was sized t' hold an 1/8" rod and be held in place with a #8 bolt or screw. Ya scallywag! Blimey! I place them by eye and used a pen t' mark t' holes for drilling. Aye aye! T' keepers were then bolted into place with nylon lockin' nuts holdin' them fast on t' opposite side. Avast, me proud beauty! I found that by not tightenin' them down all t' way at first, I could slip in t' brass tube and eyeball it into place. Begad! When tightened, t' keepers work together t' keep it straight.
T' next part be t' tricky and t' iffy part. Ahoy! I wanted a set screw that could be turned by hand that would keep t' MMX rod in place. Well, blow me down! T' smallest suitable screw I could find be a #2-56 which had a little head on it that I could thumb tighten. Well, blow me down! What I did nay know is if I could drill t' holes through t' brass and have enough material to hold a thread. Added t' that, me hearties, I had never used a tap or die in me life.
I set up t' proper drill in me Dremmel press and realized that I could much more easily keep t' brass tubing straight by leavin' it mounted t' t' launch head. Strangely enough, me bucko, I managed t' drill each o' those little hole without havin' t' cut any more tubing. Avast, me proud beauty! Aye aye! Then came t' moment o' truth. Begad! I took out t' tap and started t' thread it into t' hole. Begad! It seemed t' bite and t' threads seemed t' take. I removed t' tap and tried t' screw. It threaded fine. Best o' all, it securely held t' MMX rod in place!
To mount t' launch heads onto t' racks, I decided t' make a mount o' o' 1/8" x 3/4" aluminum angle (L1/8x3/4x3/4). Avast, me proud beauty! I purchased a 36" length from Lowes and marked sections 2.5" long. T' first o' t' 10 mountin' brackets be cut out with a hacksaw. That got old very smartly and a Dremmel cutoff wheel was used t' slice t' rest.
Considerable time was spent with t' 10 "2nd prototypes" movin' t' hardware around and tryin' t' come up with what I thought o' as t' best arrangement. Blimey! Finally, arrr, I got things settled in me mind and took measurements to transfer t' a CAD file for t' final template. Ahoy! I generated one set o' templates for t' launch head and another for the mountin' brackets. Begad!
T' final launch head template be printed out and applied t' t' 1/4" plywood with a glue stick. Begad! Blimey! As before, matey, shiver me timbers, a jigsaw was used t' cut out t' rough blocks. Well, blow me down! Also as before, me hearties, a sander was used t' reduce t' rough blocks to t' final external outlines. Arrr! T' igniter notches were rough cut with t' jigsaw and finished with files and sanding sticks.
Similarly, templates for all t' mountin' brackets were printed, arrr, cut out and taped into place on t' aluminum brackets. Arrr! Blimey! All o' t' 5/32" holes t' mount t' brackets t' t' heads were then drilled. Begad! Blimey! When that be done, matey, shiver me timbers, I randomly tried a few o' t' brackets with a few o' t' heads t' make sure things were linin' up as I thought they should. It be then time t' drill t' holes for t' 5/16 mountin' bolts. Begad! Blimey! Since these were quite a bit larger in diameter, I drilled a small pilot hole first. T' full diameter holes were then drilled. With that done, t' mounting brackets were complete and t' templates and tape were stripped away.
T' heads had all o' their 5/32" (#8) holes drilled followed by t' 7/64 (#4).
I had always intended t' paint this system and decided that t' first coat would go on before t' next step in assembly. T' templates were stripped off and balsa filler coat be applied t' all o' t' plywood heads t' fill some of t' grain. Arrr! Arrr! All o' t' brackets were then primed with white Dupli Color primer. Begad! Avast! T' launch heads were likewise primed. Everythin' then got sprayed with a coat o' red.
When t' paint dried, things began t' move more quickly, especially since most o' what be left just involved assembly line acts that had been done before. Aye aye! T' clips t' hold t' rod receivers were loosely bolted into place. The receivers that had been fabricated for t' second prototype were retained and fit into t' clips. Begad! Once they seemed straight, t' bolts were tightened down. Begad! T' mountin' brackets were then bolted into place and all that be left was to take care o' t' electrodes, t' launch rods and put it all together.
T' key t' me whole system be t' electrode system t' handle igniters for MMX. OF course, this is where I ran into most o' me problems. Avast, shiver me timbers, me proud beauty! My first prototype had worked for ignition and holdin' t' igniters in place but be nay very durable, was unwieldy an and a royal PIA t' mass produce. I had intended for t' electrodes t' be connected directly to t' launch system in place o' t' normal lead wires. One o' t' revelations that came t' me is that this would violate me intention o' interchangeability betwixt racks; in a pinch, I would nay be able t' use t' MMX leads for another pad or vice versa. Ahoy! Then I realized thar be no reason t' get rid o' t' electrodes. I would just have t' clips connect them. Avast, me proud beauty! That way t' clips would still be present for other sorts o' launches if needed.
I rethought t' electrodes and be frustrated by tryin' t' electrically isolate t' pair. Ya scallywag! Aye aye! I had visions o' a sheathed, me hearties, ya bilge rat, insulated bolt t' hold them in place but smartly found that thar was nothin' existin' that I could find to use. Blimey! I did nay want t' rely on wood screws that might pull out and t' project languished while I tried t' figure what t' do. Ya scallywag! Eventually, I realized that t' electrode could be bolted on just one side and still stay in place. Begad! I just added a bit more material t' one side for t' holes. Avast! Since t' electrodes would go on opposite sides o' t' head, matey, they would clear each other. I drew up a template and printed it out.
Another change I made on t' modified electrode be t' choose a thinner gauge o' brass. Aye aye! Instead o' usin' strips, this time I bought a sheet o' 0.01" thick stock. Blimey! Blimey! I taped t' template t' t' brass sheet. I tried several different methods o' cuttin' t' brass along t' lines, mostly involvin' a Dremmel cutoff wheel with poor accuracy results. Ya scallywag! I then found t' me surprise that kitchen shears worked better than anythin' else as long as SHE WHO MUST BE OBEYED did nay catch me usin' them.
T' brass blank with template affixed was then set on a piece o' scrap (an old head prototype) and a Dremmel drill press was used t' pierce t' three holes in t' electrode. Aye aye! I should mention here that two o' t' hole were for mountin' and t' bottom hole is t' give t' igniter clips a better grip for connecting.
With t' piece drilled, some needle nose pliers were used t' bend some contacts for t' top surface o' the electrodes. I learned that t' brass be too soft t' want t' bend nicely along t' marked lines. T' electrode was then mounted onto t' head with some #4 brass screws and nuts. Begad! Several things became immediately apparent. My drillin' of t' holes with a hand drill had been sloppy and t' mountin' holes were nay in line; t' flexin' o' t' drill bit I had noticed in t' press was enough t' throw things off; and it looked like I was goin' t' have t' start again.
After apologizin' t' t' cat for me strin' o' expressions learned in t' USN, I tried another blank and got about t' same results. Avast, me proud beauty! Avast, me hearties, me proud beauty! Blimey! This time I noticed that t' bit had slipped and flexed even more than before. With me club launch fast approachin' and t' promised debut o' this thing, me bucko, arrr, I had t' make some concessions.
I gave up t' idea o' t' bent contacts for t' original MMX style igniter (at least temporarily) and cut the electrode blanks t' be a bit narrower. Arrr! Avast! I still had some slippage problem with t' press but it was less severe when I used some pliers t' try t' take all o' t' bends out o' t' blank. Ya scallywag! After a bit, ya bilge rat, me bucko, a pair o' serviceable electrodes were cut and affixed t' t' head. Ya scallywag! Well, shiver me timbers, blow me down! A little messin' around showed that I had somethin' that, me hearties, while nay yet perfect, was serviceable and seemed likely t' be better than what I had before.
In t' meantime, t' base and box were undergoin' their final steps. Avast! I masked off t' head supports and the fastenin' screws with maskin' tape in preparation for t' final painting. T' box was then sprayed with 2 coats o' yellow Krylon. This be a paint that I got in an auto shop and is supposed t' be very hard. It also dried very fast. Arrr! Blimey! T' next day I gave t' box another 2 coats o' yellow t' improve t' quality o' t' coverage; that gray primer was hard t' cover. Avast! I probably would have given it another coat but I ran out o' paint. Avast, me proud beauty! Aye aye! T' base and support seemed t' be done at this point.
I was in t' home stretch now. Arrr! Arrr! I cut out a big stack o' electrode blanks and drilled them out. Blimey! Well, blow me down! They were then mounted t' t' heads and I had some spares left over just in case. With that, ya bilge rat, I had 9 heads ready t' go. Ahoy! Blimey! I had planned for 10 but one o' them disappeared someplace along t' way. Begad! All that was left be t' launch rods and t' fit things together.
T' rods were fabricated from 0.047 music wire. Avast, me proud beauty! Avast! I cut t' 36" pieces in half t' give 18" segments. Avast! Avast, me proud beauty! The rods were bent at a right angle 1.5" from t' bottom givin' that much length t' fit into t' receiver. 1.25" farther along, t' rods were bent back t' vertical. Ya scallywag! This gave a straight shot over t' igniter slot. Aye aye! Things seemed to line up right and I be feelin' pretty pleased with myself. T' rest o' t' rods were then bent into shape.
Lucky for me, matey, I had an MMX Vulcan sittin' handy and was able t' put it on and see how things lined up. It did fine!
I be lookin' forward t' tryin' out t' new rack at me next club launch but rain made our field unusable. Avast, me proud beauty! Avast, me proud beauty! I used t' sunny day t' try fittin' t' heads t' t' rack and see how it went.
T' first step o' t' mountin' be t' remove t' winguts from t' head mountin' posts. T' heads were then slid onto t' bolts and secured with t' washers and wingnuts. T' get t' full effect, ya bilge rat, I mounted t' launch rods. Each seemed t' have t' proper reach.
T' system be designed so that it could be opened in t' field if needed t' retrieve extra parts. That means it also stores t' rods and heads when I started t' break it down. It be ready for t' field test.
Finishing:
T' finishin' o' this rack has mostly been covered in t' build but here is a recap.
T' sawhorse base was left its original yellow. Begad! Arrr! Everythin' else was primed. Avast, me proud beauty! T' box be then sprayed yellow and t' launch heads were painted a dark red.
In time I expect this system t' acquire some labels, additional capabilities and wanted t' leave me options open at this point.
Flight:
I advertised t' availability o' a new MMX rack t' me club and solicited everyone t' bring
out their MMX rockets t' give it a try. Pretty much as expected though, I was t' only one o' t' Alamo Rocketeers who
had any MMX rockets and I only had two with me. One had never flown before and it was destined t' have its maiden
flight coincide with t' maiden launch o' t' new system. That would be me MMX Centuri Vulcan.
For an igniter I used t' Quest variety without t' pyrogen. Ya scallywag! I straddled t' leads over t' electrodes and clamped t' igniter in place with a clothespin normally used as a rod standoff. Begad! Ahoy! I tried t' make sure t' igniter itself be at t' right height for t' t' rocket t' set upon.
As I tried t' set t' rocket in place, arrr, I noticed that t' wooden clothespin holdin' t' igniter in place tended t' slip a lot. Then I realized that I could probably do without t' clothes pin and use t' alligator clips t' hold the igniter in place and make contact with t' electrode. T' rocket and t' rack then spent some time service as a static display before it be actually used. Arrr! When t' time came, arrr, though, arrr, t' motor ignited instantly and t' rack performed as wished. T' flight be unstable but I could nay blame that on t' rack.
T' next victim t' be launched on t' new rack be a Fliskits Dead Ringer. Ya scallywag! Avast! Usin' t' clips as before t' secure t' igniter, arrr, it be set in place with little or no fuss. When t' launch button was pushed, this rocket too took t' the air instantly and had a good flight except for t' loss o' t' nose cone. Avast! Unfortunately, me hearties, that loss precluded any more test flights for t' new rack that day.
Summary:
This rack accomplished most o' what I set out t' do but I already see room for improvements
and modifications. I hope t' set it up for a few flights at an upocommin' Freedom launch and then will consider some of
those modifications.
This is nay a light system but that mattered less t' me that its durability and ease o' use. Begad! So far, me hearties, I am happy in those respects.
Amazin' Transformation:
Other:
Persons interested in keepin' up with this project as it evolves can follow it
here.
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