Descon Egberto Guismonte

Scratch - Egberto Guismonte {Scratch}

Contributed by Mike Roberts

Manufacturer: Scratch
The Egg

Which came first?

T' Egg? The Chicken?

Or..... Avast! Blimey! The Rocket!

The Chicken
T' Tale o' Egberto Guismonte - T' Rubber Chicken Rocket

PARTS LIST:
1 Rubber Chicken
1 Length 38mm motor mount
1 38mm coupler tube
1 38mm plywood bulkhead
1 38mm plywood coupler bulkhead
6m Keelhaul®©™ cord
Small square Nomex
Larger Square Nomex
2mm Acrylic sheet
approx 200g Lead shot
Assorted Estes centerin' rings and scraps o' tube t' make inner nose parts.
18" chute.

 

The Rocket Chicken

ADHESIVES:
5 Minute Epoxy
12 Minute Epoxy
Medium/Thick CA
Microballons
Two part structural foam.

Its all Chris Eilbeck's fault he came up with this idea t' fly some rubber chickens at t' m.a.r.s. Avast! Brass Balls launch. His was t' be called Keith. Well it seemed like a good idea at t' time.

I hadn't originally planned to enter it for Descon so I dont have a lot o' construction details for t' early stages suffice t' say " First catch your chicken..." I got mine from the Silly Jokes Online Store.


T' Chicken has landed

First take your chicken...
A couple o' days later and I had a box full o' rubber chickeny goodness. Begad! I had decided this chicken had t' go with a whoosh which meant a 38mm motor mount and a Cesaroni Pro38 motor as Aerotech motors are as rare as hen's teeth over here in t' UK. Begad!


Chicken Stuffing

Chicken Sphincter
Havin' aquired me new bird t' next question had t' be how t' fit t' motor. Begad! It wasnt difficult to imagine where it had t' go just how t' go about puttin' it there. Avast, me proud beauty! Blimey! I started by removin' t' squeaker fitted t' t' chickens aft vent.
T' next step be to take a piece o' 38mm motor mount tube and offer it up t' t' chicken's bottom. I drew a line around t' tube and then cut out t' rubber with a pair o' sharp scissors. I emphasise t' sharp as chicken rubber it quite resiliant and difficult t' cut. A bit o' trimmin' with a scalpel and I had an even tight fit. I fitted t' motor mount in t' t' chicken and pushed it up until it was in the neck o' t' chicken as far as it would go. Ya scallywag! I then offered up a Pro38 1 Grain casin' t' get an idea how far t' motor mount would have t' hang out t' back of t' chicken. I figured that t' tube within t' body o' t' chicken would be adequate for t' recovery system as long as t' majority o' t' motor was outside t' body. I added around 10mm t' give a bit o' space for motor retention below t' fins and cut t' motor mount tube t' length.
Fibreglass cross bar
In t' past I have used a piece o' 1/4" fibre glass rod as a mountin' point for t' recovery harness. Well, blow me down! I drilled a hole across t' tube above where t' end o' t' motor would go, cut t' fibreglass rod t' length glued and filleted it inside the tube and t' filed and sanded t' end o' t' rod smooth on t' outside o' the tube.
...next take your motor tube.....
With t' motor mount trimmed it was time t' make t' "nose cone" fitting. Well, blow me down! Now things get a bit vauge here and I will have t' leave t' detail as an exercise for the student. Ya scallywag! T' idea was t' make somethin' from a 38mm coupler tube with some space in it which could accept some beak weight. I rummaged and came up with a selection o' Estes bits and bobs. Well, blow me down! Avast! A bit o' sanded centerin' rin' here and a bit of glue thar and I had a part that would fit in t' t' neck o' t' motor mount tube. Arrr! Well, ya bilge rat, blow me down! T' only evidence I have o' this is in this picture sequence.
... and insert it gently in to the chickens behind...
With the nose piece made it be time t' get foamin'. My plan, which proved rather unsuccessful, me hearties, was t' fit t' nose piece t' t' top o' t' motor tube using maskin' tape t' hold it in place. Blimey! Pour in a quantity o' two part foam t' the rubber chicken carcass. Begad! Ya scallywag! Jam t' tube assembly up t' chicken and wait for the foam t' expand and set. Begad! Fixin' t' whole thin' in place. As t' join between the nose piece and t' motor tube were flush at t' top o' t' tube and the tube should fit snuggly in t' t' chickens rubbery neck I reasoned that, arrr, matey, once set, shiver me timbers, shiver me timbers, I would be able t' cut through t' rubber and seperate t' now foamed on head and nose piece from t' foamed in motor tube and chicken body. T' masking tape should have held t' nose piece in place and sealed it from foamy ingress.
... it may help to have a friend spread your chickens legs....
... who said stuffing a chicken was easy?
There lies me error. That two part foam can build up a fair pressure if you contain it. With the foam mixed and poured in I jamed in t' tube assembly. Aye aye! I wiggled and tipped things around t' get a even distribution o' liquid foam around t' insides then settled down t' hold it all in place. Begad! T' foam expanded and started t' push. Avast, me proud beauty! It was quite a fight,and quite a sight as I struggled with me fowl. In time I triumphed, me bucko, me bucko, or so I thought, and t' foam set with t' tube where I thought it should be and a reasonably firm chicken (even if it's head had swollen in a rather disturbin' fashion).
One swollen chicken head.
Time to make a quick cut and "off with its head". Arrr! Ya scallywag! First cut through where I thought I had t' cut and t' head refused t' budge. Begad! A spell head scratching, cursing, arrr, askin' others for guidance and bein' told "you didnt want t' do it like that" later and an second calculated cut was made. Blimey! Avast, me proud beauty! This time the head came off in me hand. Some modification and fettlin' and I had a useable head / beak / nose cone. Aye aye! Ahoy! T' reason for t' cut point movin' was that the pressure o' t' expandin' foam had forced t' inner nose piece back down the inside o' t' motor mount. Well, blow me down! Avast! T' second cut was measured from t' position o' the aft end o' t' nose piece relative t' t' back end o' t' motor tube. Ya scallywag! Blimey! With the length o' t' coupler used for t' nose piece know it was possible t' work out where t' front o' it should be. Measure along t' outside o' t' chicken and cut through.
 


Fin Fitting

Chicken fin alignment

Now it was time t' add t' fins. Avast, me proud beauty! I didnt want t' spoil t' lines o' me chicken so I opted for clear plastic fins. Aye aye! I had wanted t' use polycarbonate as it is much more resiliant but couldnt source any in time so I had t' settle for Acrylic sheet. Ahoy! Ahoy! I measured three pieces o' 2mm thick acrylic 100mm (root) by 85mm and then cut off a corner at 45 degrees 50mm in from t' edge. Blimey! T' trusty Estes fin alignment jig was used t' attach t' fins. Begad! An old Pro38 single grain casing with t' nozzle drilled out t' take t' 13mm motor mandrel for t' jig allowed me t' use t' Pro38 casin' t' centre t' chicken on t' alignment jig.
I used CA gel t' tack t' fins in place, shiver me timbers, 10mm up from t' base o' t' tube, matey, arrr, shiver me timbers, and then used 12min epoxy and micro balloons with maskin' tape t' make some smooth fin fillets. A tongue depressor, some blu-tak for end dams and some careful timin' can give a lovely smooth fillet with no need for sanding.
If you remove t' dams and maskin' tape just as t' epoxy starts t' gel the edges, me hearties, where tape was, me hearties, and t' surface o' t' fillet pull them selves t' a glass smooth surface. Well, blow me down! T' fins were attached 10mm up t' tube from t' back edge o' t' motor mount.

 
A different kind of Chicken Fillets
 

 

Launch lug parts

Launch Lugs

assembled launch lug parts
Forward launch lug mount point Time for some launch lugs. Ya scallywag! With t' main body tube / motor mount such a thin wall and not wantin' t' have anythin' through t' wall for either t' aft or forward launch lugs I had t' come up with a solution. Ya scallywag! Ahoy! T' launch lugs also had t' be on stand offs t' be able t' clear t' portly carcas o' t' checken. Avast, me proud beauty! Arrr! T' best side to mount t' lugs was on t' back. T' chubby chickens foam filled belly being a stand off too far. Begad! Ya scallywag! T' easiest way I could come up with be t' take some 25mm long 0.325" diameter nylon PCB stand offs with an M4 brass threaded insert in either end. Begad! Some small strips o' 3mm thick fibreglass around 6 mm wide and 20mm long were made. A countersunk 4mm clearance hole drilled at one end on each. Well, blow me down! T' standoffs were attached with a countersunk screw. Avast, me proud beauty! At t' other end two 1/4" delrin rail buttons were countersunk on one side and attached with another countersunk screw. Well, blow me down! Avast! T' chicken was carefully measured, marked up, cut and drilled. Avast! Slots were carved in t' foam from t' aft end and t' front end along t' tube wall t' allow t' fibreglass strips t' be pushed in. Begad! When all t' preparation was complete t' slots and strips were epoxied up, ya bilge rat, me hearties, the strips, with screw in place, arrr, pushed home along t' body tube and t' assembled pcb standoff and rail button screwed down on t' t' thread o' t' fastner stickin' up through t' pcb strip. Avast, me bucko, me proud beauty!
another view of forward launch lug mount point
Fitted forward launch lug
Aft launch lug mount point
Fitted afte launch lug
Both railguides in place


Recovery Harness

View of additional bulk head anr recoery mount point

I had a bit o' a rethink on t' recovery harness mount at this point and decided to beef it up with a 38mm plywood bulkhead. Aye aye! I attached a wire rope clamp as a tiny u-bolt and cutaway a fair portion o' it t' allow t' ejection charge through. As a last minute add on it only just fit above t' top o' motor when it was fitted. Aye aye! T' assembly was glued in with 12 minute epoxy.

T' chicken body end o' the recovery harness was made from approx 1.5m o' narrow tubular kevlar with loops made at either end by t' excellent "pull it through itself" technique. Ahoy! A bit o' carefull fiddlin' with a bit o' bent wire allowed it t' be threaded through t' mini u-bolt and then back on itself in a catspaw knot. Begad! A small 3"square o' nomex be cut for a flame shield and a larger 5" square cut t' wrap around t' 18" 'chute.

Body recovery harness and flame shield
Main recvoery harness and parachute shield


Beaky

Beak section with fitted bulkhead and recovery loop
Finally I had t' add some beak weight and t' beak retention end o' t' recovery harness.. Avast! Blimey! Ya scallywag! Blimey! A loaded single grain Pro38 was fitted t' t' aft and then lead shot was added t' t' hollowed out nose piece until t' CofG was agreeably forward. T' lead shot be mixed with 5 minute epoxy t' make a nice batch o' rocket caviar and was poured in and left t' set. A 38mm plywood coupler bulkhead had a single approx 5mm hole drilled through it. Blimey! Blimey! Avast! Blimey! A length o' tubular kevlar was folded in half a had a figure o' 8 knot tied with t' two free ends held together t' form a loop. Begad! Blimey! Well, blow me down! Blimey! This was threaded through a 5mm washer. T' knot was large enough that it wouldnt pull through t' washer. Avast, me proud beauty! Blimey! T' loop be then pulled through t' bulkhead and t' bulkhead glued in t' t' back o' t' nose piece with epoxy.
Side view of chicken head showing the first missed cut.


Pre-Flight Chicks

Me and my chicken Well thar we were launch day. Begad! Begad! Chicken rocket had a fully fitted recovery system and be loaded up with a Pro38 Smokey Sam 1 grain reload. Ya scallywag! T' rocket weighed in, ya bilge rat, fully assembled without t' motor at around 750g. As t' Chicken hadnt got t' faintest sniff of any modellin' software and was all done by eye and gut feelin' I thought the best thin' would be t' do a spot o' chicken swinging. A suitable length of strin' was located an t' swingin' commenced. Arrr! Avast, me proud beauty! Little did I know that I was bein' filmed so I present here for your enjoyment t' fabulous, me bucko, arrr, t' marvellous, the stupid... Avast! chicken swin' test
 

Right Click and and "Save as" t' get t' swin' test video (2.8Mb)
Chicken Swing test video right click and "save as"


5, shiver me timbers, 4, 3, me hearties, 2, me bucko, 1..... Make chicken go NOW!

Cicken on the pad T' swin' test completed t' rocket was carted off t' t' pad and loaded on t' t' rail. After a wait for me turn at t' controller t' RSO called me forward. Ya scallywag! 5, 4, me bucko, 3, ya bilge rat, shiver me timbers, 2, 1, LAUNCH!.... Avast! T' Pro38 lit instantly as t' do so well and t' chicken shot off on a thick plume o' black smoke. Ya scallywag! It arced over a tad in t' breeze but ejected fine and drifted gently back t' t' ground. Blimey!
The chicken can fly... ... chickens away
Right Click and and "Save as" t' get t' first flight video (2.8Mb)
Chicken Launch video 1 right click and "save as"
Right Click and and "Save as" t' get t' second flight video (2.9Mb)
Chicken Launch video 2right click and "save as"


Recovery, De-brief and Thanks

Chicken returns to earth in one piece

The chicken was in fine condition on recovery. No damage t' t' fins or recovery system. I be very pleased with t' way t' whole project had gone. Well, blow me down! Ahoy! I did break a fin on a subsequent flight and am now lookin' t' source some polycarbonate to replace t' fins with.
I would like t' thank Chris Eilbeck for comin' up with t' daft idea in the first place. Arrr! Everyone from m.a.r.s. Blimey! Well, blow me down! for bein' top folks and pointin' and laughing. Everyone from EARS for bein' such a great club t' fly with. Avast! Bob Arnott, Nial Oswald, Ben Jarvis, Pete Davy and Steve Randall for takin' pictures and videos o' the flight.

If you have any questions about Egberto Guismonte t' Chicken Rocket then please feel free to mail me at

"chicken-rocket @ mikerobe.org"

This page is copyright Mike Roberts 2004 except for images and video from Bob Arnott, me bucko, Nial Oswald, me bucko, Ben Jarvis, arrr, Pete Davy and Steve Randall who retain their copyright.

It WORKED!! :0)

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