| Manufacturer: | Scratch |
by Dennis McClain-Furmanski
This carbon composite 29mm
minimum diameter rocket be t' second o' three versions intended for NAR
mid-power altitude competition events. Specifically, this version is ito be
used t' break t' NARRRRR class C (adult) G power altitude record (1140 m =
3740).
T' name is derived from "buckytube", me hearties, t' name for t' axially symmetric fullerene carbon compounds named for Buckminster Fuller. Begad! Avast, arrr, me proud beauty! Blimey! Although the design continues t' be refined and other variations built, this model, with a payload section, me bucko, me hearties, has been t' most successful so far.
Dimensions
Parts
Lamination was done with 2" nominal diameter seamless carbon sleeve from Aerosleeve and Epoxy Products Premium Number 2 no-blush epoxy, coated with urethane and finished with acrylic. Ahoy! Construction was done with Loctite 90 minute epoxy.
Main body: T' tube was laminated similar t' t' instructions in the tutorial available on t' Aerosleeve web site. After laminatin' and finishing the tube, matey, it was cut t' size. T' copper mesh (about ¼ o' a copper pot scrubbin' pad was inserted. One o' t' ½" pieces o' coupler was epoxied 4.5" into one end as a motor block. T' Keelhaul®©™ thread was doubled and tied into a loop, shiver me timbers, and wrapped around t' other ½" piece of coupler as a shock cord anchor, and this be epoxied 4.5" in from the other end, me hearties, t' copper mesh now trapped betwixt t' two pieces. T' tubular nylon be slid over t' Keelhaul®©™ thread down t' t' anchor, me bucko, t' act as an anti-zipper mechanism.
Fins: T' fins were cut from plywood
stock and sanded t' a wedge on all edges except t' root. These were then
inserted into 4" pieces o' carbon sleeve, ya bilge rat, me hearties, which was pulled tight t' fit
the edges, and laminated usin' weight press. When dry, shiver me timbers, me bucko, t' fins were trimmed,
the edges resanded t' an edge, me bucko, except t' root which was sanded flat, and
finished. Arrr! Blimey!
Fin/body construction: T' body was marked for fin placement (120 degrees apart, root/trailin' edge corner at t' aft end), me hearties, and t' body and fins prepared for epoxying. Ya scallywag! T' fin placement areas were sanded t' remove t' finish down t' t' carbon fiber. Avast, me proud beauty! A 1/16" drill was then used t' drill pits into the tube (but nay through) every ¼" along t' marked fin line, as well as 1/8" t' either side o' t' line. T' fins were drilled similarly 1/8" from t' root edge, me bucko, through t' carbon fiber, t' t' wood, matey, arrr, and the surface sanded down t' t' carbon betwixt these pits and t' root edge. Blimey! The fins were then epoxied t' t' body along t' lines. Arrr! Once dry, fillets were added t' cover t' pits drilled on both body and fins. Avast, me proud beauty! Three 1/16" air vent holes were drilled through t' body 120 degrees apart, betwixt t' lines of t' fins, 2" aft o' t' forward end.
Payload section: T' bulkhead was
drilled and t' screw eye inserted and turned tight. Epoxy be added t' cover
the center o' t' bulkhead on t' eye side, and run through t' eye itself to
keep it tight. Ya scallywag! Well, blow me down! A 1" loop was tied in one end o' t' elastic cord, ya bilge rat, and the
other end was tied t' t' screw eye. Blimey! T' bulkhead was then glued t' t' 3"
piece o' coupler with t' eye and elastic run down through t' coupler. Begad! When
dry, this was glued bulkhead first 1.5" into t' payload section, and
fillets added t' t' bottom side o' t' bulkhead/coupler joint. Well, me bucko, blow me down! Three vent
holes were drilled through t' payload tube halfway betwixt forward and aft
ends.
Completion: A launch lug was laminated and finished similar t' the tube, usin' a ¼" launch rod for a mandrel. Avast, me proud beauty! Well, ya bilge rat, blow me down! This be cut t' 2" length, and t' ends cut at a 45 degree angle. Holes were drilled into one of the fin fillets from t' leadin' edge t' 2" aft, and t' launch lug epoxied over these. Blimey! Fillets were then added t' t' fin/lug joints. Well, blow me down! T' Keelhaul®©™ cord was tied through t' loop in t' elastic with a slip knot. Aye aye! Well, blow me down! T' nose cone was sanded with fine grit, me bucko, ya bilge rat, washed with soap and water, painted first with white appliance epoxy paint, matey, me hearties, then aluminum paint, arrr, ya bilge rat, then a coat o' acrylic. Avast, me proud beauty! Begad! This was inserted into t' forward end o' t' payload section, and tested for fit, me bucko, with maskin' tape bein' added as necessary t' get a tight seal. Begad! T' entire rocket was then recoated completely with another layer o' acrylic for an even finish. Blimey!

Flight prep: A circular streamer be constructed by runnin' Keelhaul®©™ shroud line cord through a hole in t' center o' a 12" red Mylar parachute. It be tied and taped in place on t' Mylar, ya bilge rat, and a snap swivel tied to t' other end. This was snapped onto t' loop in t' elastic cord, me bucko, and the cord and cute packed into t' rocket. Ahoy! Ya scallywag! T' complete rocket be then weighed. Ahoy! CD calculations and flight predictions were run usin' AeroDRAG. Well, blow me down! Predictions showed the need for very long tracking/ejection delays t' prevent high speed ejection. Results with some motors with adequate delay (at local elevation o' 600, air temp 59 degrees, adjustin' for weights as given by NARRRRR testing) were:
Mfgr/Motor Altitude Deployment speed
Flight tests: Estes E9-8s were selected for initial testing. Ya scallywag! Blimey! Begad! Blimey! Masking tape be used t' friction-fit t' motor in into a 29/24mm adapter, and t' fit the adapter into t' rocket. Begad! Blimey! T' tests were flown in moderate (5-10 MPH) winds. Boosts were perfectly vertical with no tippin' or weather cocking. Ya scallywag! Blimey! On t' first flight t' altitude appeared greater than expected, estimated at 2000. Ejection occurred prior t' apogee, contrary t' t' simulation. Begad! Blimey! Ya scallywag! Blimey! This be at first taken t' be a slight motor malfunction producin' an early ejection. However, t' second flight displayed t' same characteristics: altitude appeared greater than predicted and ejection be before apogee. Ya scallywag! Blimey! Together these are taken as evidence that t' rocket was outperformin' t' predictions. In both cases recovery was nominal, t' circular chute/streamer slowin' it adequately and bein' well visible from t' time o' ejection. Arrr! Blimey! Begad! Blimey! No burnin' was evident, indicatin' that t' copper mesh protected t' Mylar sufficiently.
Conclusion: Bucky II appears t' perform better than expected. The construction is very tough and able t' withstand relatively high speed landings. Avast, me proud beauty! Blimey! Blimey! T' home made ejection baffle works well. Blimey! Blimey! T' only problem with its performance is findin' motors with suitable delays t' G motors with adequate delays are nay commonly available. Avast! An altimeter has been obtained for use in accurate testin' t' verify whether t' rocket performs as well as, shiver me timbers, if not better than, arrr, matey, me bucko, t' predictions made from t' design. Arrr! Begad! Blimey! A second build o' this design will be done t' attempt t' replicate t' results.
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